67hat34c
Legendary Member
- Joined
- Apr 18, 2005
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- 1,929
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- Hatteras Model
- Not Currently A Hatteras Owner
In prior posts i have discussed recent trouble with one of our crusader model 350's. we had the carb rebuilt, i pulled intake and installed new lifters, got all adjusted well and ran her. ran fine except it would not turn more than 3700, did not race up and die or sputter or anything else, just would not go any faster. port motor ran up to 4000 and ran fine. guess starboard motor not turning up caused port to hold at 4000 instead of 4400.
got to boat friday night and went through starboard motor again, cked throttle linkage and it was wot. checked running volts to coil and it was 13.00 checked timing and it was fine, looked to see if advancing and it was fine. pulled the plugs and noted all black except #5 it was clean, not even burnt. now these plugs only have a couple of hours on them, changed when i did the carb and lifters. someone on the dock suggested it was a bad spark plug and we had dead cylinder. oh also i rechecked all compression and all were between 162 and 165lbs, same as they were in may when ckecked last time. anyhow i decided to go fishing next day and run on 15cyl as we have apparently been doing this for a while now. well we hit the inlet and gave it the juice and the thing backed fired and sputtered etc. backed off and turned around and headed back. gave wheel to dad and went down and pulled deck open, saw spark coil wire off with flame /arc so i shut it down to re attach and found it soaked with oil, blown coil. went back to the dock and changed the coil and also tested the a few cyl by pulling off the plug wire, #1 slowed it down, #3 slowed it down, #5 nothing. changed that plug and it made no difference. ok bad wire. (msd 8mm wires changed about 3 yrs ago) well we fished, got 4 barracuda and one dolphin and came back. pulled wire and took it home. Put wire on ohm meter and it seems fine.
WTF is going on ? is wire breaking down at higher temp? possible not attached to plug properly as it is hard to get to behind the oil dip stick tube?
the wire lights up the timing light before the spark plug boot. of course that does not mean there is enough juice to light the plug i guess.
Going to get a couple of new wires and check it again possibly friday.
side issue, amazing how much stuff you find wrong when something quits working properly. none of it related but all needed attention. lucky that there is not a major mechanical issue. very happy with compression although dont know why so high, by the way have run a couple of cans of sea foam through it since may when this all first came to a head. thought that would have cleaned up cyl and lowered compression a little.
by the way the first compression stroke on each cyl shot the compression way up very fast, the rest of the strokes got it the rest of the way a little at the time. i take it that this is good.
got to boat friday night and went through starboard motor again, cked throttle linkage and it was wot. checked running volts to coil and it was 13.00 checked timing and it was fine, looked to see if advancing and it was fine. pulled the plugs and noted all black except #5 it was clean, not even burnt. now these plugs only have a couple of hours on them, changed when i did the carb and lifters. someone on the dock suggested it was a bad spark plug and we had dead cylinder. oh also i rechecked all compression and all were between 162 and 165lbs, same as they were in may when ckecked last time. anyhow i decided to go fishing next day and run on 15cyl as we have apparently been doing this for a while now. well we hit the inlet and gave it the juice and the thing backed fired and sputtered etc. backed off and turned around and headed back. gave wheel to dad and went down and pulled deck open, saw spark coil wire off with flame /arc so i shut it down to re attach and found it soaked with oil, blown coil. went back to the dock and changed the coil and also tested the a few cyl by pulling off the plug wire, #1 slowed it down, #3 slowed it down, #5 nothing. changed that plug and it made no difference. ok bad wire. (msd 8mm wires changed about 3 yrs ago) well we fished, got 4 barracuda and one dolphin and came back. pulled wire and took it home. Put wire on ohm meter and it seems fine.
WTF is going on ? is wire breaking down at higher temp? possible not attached to plug properly as it is hard to get to behind the oil dip stick tube?
the wire lights up the timing light before the spark plug boot. of course that does not mean there is enough juice to light the plug i guess.
Going to get a couple of new wires and check it again possibly friday.
side issue, amazing how much stuff you find wrong when something quits working properly. none of it related but all needed attention. lucky that there is not a major mechanical issue. very happy with compression although dont know why so high, by the way have run a couple of cans of sea foam through it since may when this all first came to a head. thought that would have cleaned up cyl and lowered compression a little.
by the way the first compression stroke on each cyl shot the compression way up very fast, the rest of the strokes got it the rest of the way a little at the time. i take it that this is good.