rustybucket
Legendary Member
- Joined
- Jul 12, 2013
- Messages
- 1,200
- Status
- OWNER - I own a Hatteras Yacht
- Hatteras Model
- 52' CONVERTIBLE (1983 - 1990)
Hey guys, sorry I have been mia for a while, business got REALLY busy and pulled me away from the boat for a few months. Probably best b/c I could definitely feel a little burnout coming on.
Long story short, we went down to do a seatrial (first real one since being back on the water) about a month ago. Had a very bad vibration on stbd side, so much so that I didn't really want to get her up on plane. So we limped back home and started scheduling a quick haul.
I've always felt like we had a vibration on the boat somewhere, but I never could put my finger on it.
So we haul out, props look mint, pull the props off and setup clamping dial indicators at various points along the shafts and sure enough, stbd side was showing 12 thousands wobble. Port was showing 3 thousands.
So we pulled both shafts and carried them over to Whistler in Mobile.
Here is the homemade puller we used to pop the couplings off, worked like a dream.
Got all the brand new paint off the shafts with a knotted wire brush on a big dewalt grinder. Used a chain hoist and big ratchet straps to pull the shafts out. Two of us (helper in pic) pulled them and loaded them up in the excursion. I would not suggest 2 people trying to do this project, these 2.5" shafts are HEAVY!!! I'd guess 400-500lbs easy.
After we got the shafts out we cut out all 6 of the cutlass bearings. Actually 2 we didn't have to cut, were able to drive them out. We used a 12" Diablo carbide tipped sawsall blade labeled for 'thick metals'. I've cut out cutlass bearings before but the diablo carbide was a very consistent controlled cut and the saw had a lot of backbone so it made cutting at the tip a breeze. Highly recommend this $30 blade if you gotta do this project. We stripped out the piece of bearing rubber everywhere we cut so we could get a good visual on the cut.
Long story short, we went down to do a seatrial (first real one since being back on the water) about a month ago. Had a very bad vibration on stbd side, so much so that I didn't really want to get her up on plane. So we limped back home and started scheduling a quick haul.
I've always felt like we had a vibration on the boat somewhere, but I never could put my finger on it.
So we haul out, props look mint, pull the props off and setup clamping dial indicators at various points along the shafts and sure enough, stbd side was showing 12 thousands wobble. Port was showing 3 thousands.
So we pulled both shafts and carried them over to Whistler in Mobile.
Here is the homemade puller we used to pop the couplings off, worked like a dream.

Got all the brand new paint off the shafts with a knotted wire brush on a big dewalt grinder. Used a chain hoist and big ratchet straps to pull the shafts out. Two of us (helper in pic) pulled them and loaded them up in the excursion. I would not suggest 2 people trying to do this project, these 2.5" shafts are HEAVY!!! I'd guess 400-500lbs easy.

After we got the shafts out we cut out all 6 of the cutlass bearings. Actually 2 we didn't have to cut, were able to drive them out. We used a 12" Diablo carbide tipped sawsall blade labeled for 'thick metals'. I've cut out cutlass bearings before but the diablo carbide was a very consistent controlled cut and the saw had a lot of backbone so it made cutting at the tip a breeze. Highly recommend this $30 blade if you gotta do this project. We stripped out the piece of bearing rubber everywhere we cut so we could get a good visual on the cut.

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