Genesis
Legendary Member
- Joined
- Mar 28, 2005
- Messages
- 5,952
- Hatteras Model
- 45' CONVERTIBLE-Series II (1984 - 1992)
Seriously.
I don't know if my deal is with the guy in the white robes or the red suit, but I'll take whichever it is.
After our aborted trip to the Angelina last week (a wreck we intended to dive which was called due to a line of boomers bearing down on us) I decided to pull down the coolers on the starboard engine and have them cleaned, as the port (which I did) was running nice and cool and the other a bit warmer.
No big deal, other than waiting for Saunders to get me the new seals and gaskets that I needed to finish the job (remind me to shoot them sometime)
Anyway, I put it all back together and lit it off the other night. Flawless.
So this morning I tool over to the boat to clean up the mess. See, when you pull the blower on a Detroit Diesel, oil goes EVERYWHERE. Its unavoidable. This, of course, make a hellish mess in the engine room, which you then need to clean up. So to the boat with the steam cleaner and rags I go, along with a gallon of simple green and a slop bucket to wetvac the mess into.
I get there and happen to glance down into the OTHER (port) engine's drip pan. There's a bit of coolant in there. Now, this is an engine that was NOT touched. There shouldn't be ANYTHING in that pan. At all.
Coolant leaks are not a good thing. So I start feeling around looking for what's wet. I find it - its a fitting on the bottom of the main elbow coming from the heat exchanger back to the water pump. Ok, so its gotten a bit loose I think to myself. I reach for a 9/16", touch the fitting, and it breaks off in my hand.
Oh shit.
I now have a finger in the dike (literally) keeping the green firehose from spraying all over. I managed to find a bolt and a piece of oil rag that would stanch the flow to a dribble while I grabbed two 5 gallon buckets, hoses, and funnels (which I had on board as I just finished draining the OTHER side to do the work on it!), and opened the other drain valve to get the coolant out of the engine.
I then examine the fitting that I have half of in my hand, and discover that there is a crack that has been there for quite some time (probably since installation about a year ago) which apparently had propagated all the way around! It looks like a casting defect to me, as there's no evidence of it shearing due to torque or other loads. (A year or so back I replaced the drain cocks on the elbows and oil coolers with fittings and ball valves with a hose barb on the end, to make draining the cooling system a non-eventful thing. I remove the handles when not in use so I don't accidentally drain the contents of the system while underway!)
Anyway, the rest of the fitting is broke off flush (of course) and the fitting IT is screwed into won't come off the elbow (cast iron .vs. brass, not a good combination after 20 years.) So I pull the elbow, get my Easyouts, hammer in the appropriate one, and extract the piece of the nipple that was still in there. Then I get to make a new gasket out of gasket paper as I don't happen to have one of those laying around, change the hose to which it was connected (just for good measure), and stuff it all back together with a new 97 cent nipple.
There went four hours of work, including the cleanup of THAT mess.
However - if that had failed offshore 20nm+ out, dumping the entire cooling system into the bilge, that engine would have almost certainly been destroyed. Once the temperature sensor is uncovered you get no warning of the overheat-in-progress until you either get a fire or a seizure 90+% of the time. Since the breach was directly in front of the waterpump, it would have been catastrophic and dumped the entire system inside of 30 seconds, as it would have been pumping under full system pressure.
I estimate that another couple of hours of engine runtime and it would have cracked right off. No doubt about it.
I dodged a major bullet here... best case is I would have had to come in on one engine. Worst case is that I would have trashed the other engine at the same time, and Gig would have been out of service for at least 2-3 weeks for a rebuild, with a parts cost alone (if I did all the work) exceeding $10k.
As it was, the damage was 97 cents.
I'll take it... now I know the call I made Friday was the right one, even if not for an obvious reason ......
Lesson? Always look in the engine room and if something doesn't look right, it isn't. Find out what's up before you get an expensive surprise!
I don't know if my deal is with the guy in the white robes or the red suit, but I'll take whichever it is.
After our aborted trip to the Angelina last week (a wreck we intended to dive which was called due to a line of boomers bearing down on us) I decided to pull down the coolers on the starboard engine and have them cleaned, as the port (which I did) was running nice and cool and the other a bit warmer.
No big deal, other than waiting for Saunders to get me the new seals and gaskets that I needed to finish the job (remind me to shoot them sometime)
Anyway, I put it all back together and lit it off the other night. Flawless.
So this morning I tool over to the boat to clean up the mess. See, when you pull the blower on a Detroit Diesel, oil goes EVERYWHERE. Its unavoidable. This, of course, make a hellish mess in the engine room, which you then need to clean up. So to the boat with the steam cleaner and rags I go, along with a gallon of simple green and a slop bucket to wetvac the mess into.
I get there and happen to glance down into the OTHER (port) engine's drip pan. There's a bit of coolant in there. Now, this is an engine that was NOT touched. There shouldn't be ANYTHING in that pan. At all.
Coolant leaks are not a good thing. So I start feeling around looking for what's wet. I find it - its a fitting on the bottom of the main elbow coming from the heat exchanger back to the water pump. Ok, so its gotten a bit loose I think to myself. I reach for a 9/16", touch the fitting, and it breaks off in my hand.
Oh shit.
I now have a finger in the dike (literally) keeping the green firehose from spraying all over. I managed to find a bolt and a piece of oil rag that would stanch the flow to a dribble while I grabbed two 5 gallon buckets, hoses, and funnels (which I had on board as I just finished draining the OTHER side to do the work on it!), and opened the other drain valve to get the coolant out of the engine.
I then examine the fitting that I have half of in my hand, and discover that there is a crack that has been there for quite some time (probably since installation about a year ago) which apparently had propagated all the way around! It looks like a casting defect to me, as there's no evidence of it shearing due to torque or other loads. (A year or so back I replaced the drain cocks on the elbows and oil coolers with fittings and ball valves with a hose barb on the end, to make draining the cooling system a non-eventful thing. I remove the handles when not in use so I don't accidentally drain the contents of the system while underway!)
Anyway, the rest of the fitting is broke off flush (of course) and the fitting IT is screwed into won't come off the elbow (cast iron .vs. brass, not a good combination after 20 years.) So I pull the elbow, get my Easyouts, hammer in the appropriate one, and extract the piece of the nipple that was still in there. Then I get to make a new gasket out of gasket paper as I don't happen to have one of those laying around, change the hose to which it was connected (just for good measure), and stuff it all back together with a new 97 cent nipple.
There went four hours of work, including the cleanup of THAT mess.
However - if that had failed offshore 20nm+ out, dumping the entire cooling system into the bilge, that engine would have almost certainly been destroyed. Once the temperature sensor is uncovered you get no warning of the overheat-in-progress until you either get a fire or a seizure 90+% of the time. Since the breach was directly in front of the waterpump, it would have been catastrophic and dumped the entire system inside of 30 seconds, as it would have been pumping under full system pressure.
I estimate that another couple of hours of engine runtime and it would have cracked right off. No doubt about it.
I dodged a major bullet here... best case is I would have had to come in on one engine. Worst case is that I would have trashed the other engine at the same time, and Gig would have been out of service for at least 2-3 weeks for a rebuild, with a parts cost alone (if I did all the work) exceeding $10k.
As it was, the damage was 97 cents.
I'll take it... now I know the call I made Friday was the right one, even if not for an obvious reason ......
Lesson? Always look in the engine room and if something doesn't look right, it isn't. Find out what's up before you get an expensive surprise!